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  1. mtltemplar

    Head gasket replacement

    So I don't have a 31mm socket (of course), just a 30 and 32, but the 32 was close enough to at least give it a shot - put a normal socket wrench on there and tried to 'tighten' it, and it just turned the crank over, no tightening of the bolt that I can tell. I went ahead and gave it a full...
  2. mtltemplar

    Head gasket replacement

    So does one seriously have to drain the cooling system, remove the coolant reservoir and disconnect hydraulics and remove the rad fan before being able to remove the crank pulley and/or check the crank bolt? Seems like there's just enough room for a wrench and socket in there (barely) but if you...
  3. mtltemplar

    Head gasket replacement

    No worries, you couldn't have known, sorry I didn't mention it in my first post. I'm going to try to take the pulley off tomorrow night and start checking out the balancer. Is there room in there to use an impact wrench to get the crank bolt off or how do you suggest bracing things to keep the...
  4. mtltemplar

    Head gasket replacement

    I've looked from on top and up from below and all the pulleys seem to be in alignment, none of them farther away/closer to the engine than the rest, thus I hadn't gone to the trouble of removing the crank pulley and checking the balancer. I would hate to have to remove and re-torque that bolt...
  5. mtltemplar

    Head gasket replacement

    Do I replaced the thermostat, temp sensor and auto tensioner/belt. Getting ready to start bleeding when I notice it seems the belt has jumped one rib up onto the edge of the P/S pulley, but only on that one, the rest of them it's in the right place... With the new tensioner, that shouldn't be...
  6. mtltemplar

    What's this noise?

    Guess something is still wrong... Need to buy the new tensioner I guess - still hadn't done that yet. Went to work my overheating issue today (replacing thermostat and temp sensor) and see this - and that was on a brand new belt that I put in there at the end of October.
  7. mtltemplar

    Head gasket replacement

    That would suck if it's just an intermittent issue, but at the same time it was fine all year until I turned on the heater again for the first time, so one can always hope it's something simpler... :)
  8. mtltemplar

    Head gasket replacement

    So... finally rustled up the $217 it took to 'rent' the cooling system pressure tester kit from Advance. With the system off and cold, installed the pressure tester, pressurized to 16 PSI (what's on the rad cap) and left it for a couple minutes with 0 pressure loss. Then I released the pressure...
  9. mtltemplar

    Head gasket replacement

    Finally got some time off work to test stuff out: Uncapped the rad, unscrewed the bleeder valve and a small, and I mean *small* amount of air came out, nothing more, just fluid after that. Ran the truck, disconnected the electrical sensor when it started to warm up, fan kicked into high almost...
  10. mtltemplar

    Head gasket replacement

    My truck has been having overheating issues off and on for a couple years. When it pegged the gauge a couple times I took it to the shop and they did a coolant flush and found a bunch of air in there. After that it didn't overheat again for the last 9 months until I started using the heater...
  11. mtltemplar

    What's this noise?

    So after about 4 days the squeaking came back some... But only at WOT, otherwise it doesn't happen at idle. So I'm guessing I need to replace the tensioner still, Napa doesn't have one for this truck. Has anyone used the one from Rock Auto? It's less than half the cost of OEM from Dodge.
  12. mtltemplar

    What's this noise?

    So, replaced the idler pulley, sound went away when rpms were increased but was still there at idle. Replaced the belt, sound went away completely. But... that said, last time the belt was replaced this happened and it came back a couple days later. I'm still gonna check the balancer and crank...
  13. mtltemplar

    What's this noise?

    I'm gonna need to go stuff some sponges in the spark plug hole now to soak up the excess after I get the rope fished back out, the 'tail' fell in... I knew the water was trolling, obviously, but that rope in the cylinder almost sounded legit enough that I was wondering, I'm thinking, seriously...
  14. mtltemplar

    What's this noise?

    So not just me then, huh?
  15. mtltemplar

    What's this noise?

    Wow, I feel like I'm being trolled... ;) I realize I probably sound like a noob, and I probably am in many ways, but seriously? Rope in the cylinder? LOL
  16. mtltemplar

    What's this noise?

    vprpwrd, email sent. :) Thanks Ok, I'll definitely still check it out, can't hurt - just to be safe. Better a 'quick' check than a new crank... So, the question still stands, how do I backstop the crank so I can torque said bolt to 130 ft.lbs? Seems to me that an automatic can't be engaged like...
  17. mtltemplar

    What's this noise?

    Geezuz, man I hope mine isn't that bad. I tried taking off the belt and hand spinning all the pulleys, no noise (even tried using the belt wrapped around them and yanked to get them spinning faster, still nothing). Did notice the belt tensioner is pretty rusted internally, and its pulley stops...
  18. mtltemplar

    What's this noise?

    Hey, not sure if general discussion is the right place for this, or if this is even a tech discussion forum... If both are correct though, any guesses on what this sound is? Took it to Dodge and they originally said it was the belt and replaced it, and the sound went away for almost 3 days then...
  19. mtltemplar

    Rough running, possible water problem?

    Reply I wish to god that it were that easy... ;) I have tried all angles, barely in, all the way out, gave it the lovin... Nothing helped. Already tried a gas container as well, but it still overflows and I have to stop pouring. There is nothing stuck in the fill hose, already took that off...
  20. mtltemplar

    Rough running, possible water problem?

    Update So, I have no engine codes. I put in some injector cleaner which helped with the rough running some (so possibly bad gas), also disconnected the battery for 2 hours and now it seems to be almost perfect again, from that aspect. It still occasionally misses but it is nowhere near as...
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