rare03srt10
Full Access Member
Alright so i took the truck over to my roommates shop this weekend and we changed out the stock fuel pump to SRT10 spec because the truck wasnt running right so we figured with the srt10 pump running more PSI would help. Well the truck runs worse lol. We hooked it up to the dyno to check air/fuel and unfortunitly his wideband plug got smushed so we werent able to check air/fuel but decieded to take a pass anyway to see the graph and some numbers. Well at part throttle the truck doesnt wanna run at all. It you give the truck anything less then half throttle it falls on its face BAD, but at full throttle it clears out and feels good but still isnt making power. Truck made 369 horsepower and 395 torque. Heres a video of the pull:
[ame=http://www.youtube.com/watch?v=tlbLP-IxkNo&feature=youtube_gdata_player]Srt10 runnin waay to rich and lots of timing‏ - YouTube[/ame]
Do you guys think that the B&G tune is just way to rich or has waay to much timing? We still need to put it on the dyno to check air/fuel out but i can tell you that my plugs are looking pretty rich.
Oh and by the way i didnt print the graph but we took two pulls and the graph is VERY consistant and smooth
[ame=http://www.youtube.com/watch?v=tlbLP-IxkNo&feature=youtube_gdata_player]Srt10 runnin waay to rich and lots of timing‏ - YouTube[/ame]
Do you guys think that the B&G tune is just way to rich or has waay to much timing? We still need to put it on the dyno to check air/fuel out but i can tell you that my plugs are looking pretty rich.
Oh and by the way i didnt print the graph but we took two pulls and the graph is VERY consistant and smooth